Hi all
Further
to Ken Gebhart and Geoffrey Kolbe suggestions I succeeded in extracting
the Bubble Illumination Assembly that was stuck in the instrument body.
I
first proceeded in taking off the front glass window which gave access
to the bulb. I then relatively easily extracted the bulb with a small
pair of pliers from this opening. This is rather delicate because one
has to squeeze the bulb to induce a rotation movement in its tapping
without braking it.
I thereafter had a partial access to the front end of the light assembly.
I
then proceeded to take the black rheostat cap off which enabled me to
confirm that fortunately there was no old battery present in the tube.
The
next step was to find a way to push the tube out of its housing. I used
an adjustable clamp actuated by a screw actuator and resting on the
front end of the light assembly on the zinc casting and resting on the
bottom side on a fixed part of the sextant body. This way I imposed a
pressure on the front end of the light assembly and more precisely on
the zinc casing. The tube almost instantly unstuck and was pushed 15mm
(0.6 inches). Unfortunately the tube would not slide down any further
and seemed to have hit a stop in its travel and to have got locked in
this new intermediate position.
I
then had to add an extension arm between the clamp top side jaw and the
zinc casting in order to be able to go on developing a downward
pressure. Sadly at this moment the top of the zinc casting fractured
and the tube was still stuck in its bore.
The next step was
to pour a lot of penetrating oil in this area and try to move the now
protruding bottom side of the tube by hand. I also used a pliers at one
time on the protruding bottom side of the tube but quickly stopped
because the thin walled tube could not withstand the smashing force
induced by the tool and got locally deformed. I resumed pouring
penetrating oil and working the light assembly back and forth in its
bore to induce shocks on the stop and it suddenly came out.
The
consequence is that I saved the rheostat and the tube part of the light
assembly (had to put it back locally in a cylindrical shape to even out
the pliers prints). Both components are fully usable now. Sadly the
original zinc casting is destroyed beyond repair, but it can easily be
duplicated on a lathe in any conductive material. I am currently
thinking of brass or aluminium if I cannot find zinc.
The
origin of the problem does not seem to have been a question of
corrosion or galvanic couple, but as Ken Gebhart stated, a question of
geometrical expansion of the zinc cast diameter.
My special thanks to Ken Gebhart and Geoffrey Kolbe for their precious advices and valuable help.
JPP